Read an Excerpt
  Proceedings of the 3rd International Gas Processing Symposium 
 5–7 March, 2012, Doha, Qatar 
 Elsevier 
 Copyright © 2012   Elsevier B.V. 
All right reserved.
 ISBN: 978-0-444-59501-0 
    Chapter One 
  Exercising the Option of CO2 Slippage to Mitigate  Acid Gas Flaring During SRU Expansion Bellow  Failure    Jaber Shafah  
  
  Abstract  
  In the Claus process Sulphur Recovery Units, metallic bellow expansion joints in the  tail gas line to Incinerator, seldom fail by developing crack on the bellow element due to  various mechanical and metallurgical reasons.  
  Any such bellow failures are irreparable and it demands replacement of the entire  expansion bellow assembly which is a long lead item. Though the Incinerator operates  at a negative pressure, tail gas inlet line used to have a slight positive pressure  proportionate to the volumetric flow rate of tail gas that will cause the harmful toxic tail  gas to leak through the cracked bellow creating an HSE hazard. To prevent the above  leakage, SRU unit will be forced to operate at reduced throughput rates by flaring Acid  gas from the upstream Acid gas removal units until replacement of the bellow joint  which will cause a serious impact on the environment and result in loss of sulphur  production.  
  Exploiting the Selective absorption characteristic of absorbent (Methyl-Di-  Ethanolamine) used in Acid gas removal units has been successfully undertaken in  Qatar Petroleum's NGL-3 Plant in order to eliminate the prolonged, anti-environmental  Acid gas flaring and to curtail the loss of sulphur recovery forced by the above situation.  Detailed description of the attempts and actions taken towards the above task execution  to minimize Acid Gas flaring without violating the AGRU product specs and without  further deteriorating the leaking expansion bellow are covered in detail below with the  details of benefits realized.  
  Keywords: Crack, Bellow Failure, Leak, CO2 Slippage, Selectivity, SRU Management.  
  
  1. Introduction  
  1.1. Technical background  
  Qatar Petroleum's NGL-3 plant Gas Sweetening Facility treats 1020 mmscfd of Non-associated   Natural gas containing approx. 0.6 % H2S and 2.4 % CO2 in two trains of  Acid gas removal units (AGRU) using aqueous Methyl Di-Ethanolamine (MDEA)  solution absorbent. Recovered Acid gas is processed in a single train Sulphur Recovery  Unit (SRU) with two catalytic conversion stages.  
  The above SRU, designed on the basis of modified Claus process, is equipped with a  tail gas Incinerator of natural draft, sub-atmospheric pressure type thermal incinerator  with air flow controlled using burner air registers. Tail gas inlet line to the incinerator is  installed with a Tied Universal type metallic bellow expansion joint to accommodate  line expansion and movements. This expansion joint made out of Inconel-65 metallurgy  was in operation since Year 2005 which subsequently during May-2011 had developed  a crack on the metallic bellow element and started leaking toxic tail gas to atmosphere.  
  
  1.2. Tail gas line Bellow failure and Consequences  
  In general, weld repair of any cracked metallic bellow is not recommended, as it is not  possible to restore the original bellow functionality after repair. That will further  jeopardize its operational integrity. Therefore it is always considered safe to replace the  entire expansion joint bellow assembly from the reliability point of view. Procuring a  new bellow joint for replacement normally takes a minimum of 10 to 14 weeks subject  to the supplier / manufacturer constraints. Shutting down SRU totally and flaring Acid  gas for extended periods until the replacement of bellow is not permitted as it is anti-  environmental.  
  Acid gas feed to SRU when reduced by 15% (from 17.05 mmscfd to 14.45 mmscfd)  found creating less back pressure in the tail gas line that immediately led to temporary  stoppage of leak. In order to avoid further degradation of leaking expansion bellow and  to eliminate the likelihood of any toxic gas emission to atmosphere and untoward  incidents, unit has been kept operating with reduced throughput rate. Sustained  operation of SRU with reduced feed rate until replacement of bellow has negative  consequences such as flaring partial amount of produced Acid gas to atmosphere which  mounts to an estimated at 300 mmscf and loss of approximately 2600 tons of Sulphur  product for the total estimated period required for new bellow procurement.  
  
  2. Methodology to minimize Acid Gas Flaring  
  2.1. Limitations restricting control of Acid gas loading  
  Total volume of Acid gas produced from Acid gas Removal unit is a function of total  amount of H2S and CO2 absorbed into the amine stream towards achieving the treated  gas specification requirements. To prevent or minimize Acid gas flaring without  reducing the total Raw gas feed to the plant in the situation described above, controlling  the acid gas loading of the amine in order to allow CO2 slippage in the treated gas has  been chosen as a safe and economical option, provided the treated gas specification  limits should not be violated.  
  Treated gas H2S content specification of 4 ppm vol. can never be violated whereas the  CO2 content limit of 1% vol. can be marginally deviated without violating the  specification limit of Ethane rich gas supplied to Ethylene crackers and Lean gas  supplied to the Industrial consumers.  
  Presence of excessive CO2 in the sweetened feed gas to cryogenic section possibly leads  to formation of Dry Ice, most probably over the trays below the feed tray of De-  methanizer column where conditions are favorable for CO2 to reach stages of top  equilibrium concentrations rather than at expander outlet conditions. Close monitoring  of column differential pressure and other operating conditions is necessary for early  identification of any onset of CO2 solidification.  
  
  2.2. Manipulating the Selectivity to control Acid gas loading  
  Acid gas loading of Amine is a function primarily based on two variables such as amine  circulation rate and the contact time. As the inlet raw gas feed composition remains  constant, total volume of acid gas picked up by the amine can easily be reduced by  changing amine circulation rate. Whereas any amount of reduction in amine circulation  rate has a direct negative impact on the treated gas H2S content and hence reducing  amine circulation rate has been ruled out.  
  Manipulating with the selective absorption characteristic of MDEA is the only key  parameter to be manipulated here for reducing the Acid gas pick up rate in order to  achieve the above requirement. Being a tertiary amine, MDEA reacts slowly with CO2  and has only a moderate absorption rate. As the selectivity towards absorbing H2S is  achieved by differences of reaction rates between H2S and CO2 with MDEA; reducing  CO2 absorption can be accomplished by appropriately reducing the amine contact time  which must be long enough to absorb almost all the H2S, but sufficiently short to  remove only partial amount of CO2.  
  
  2.3. Increasing CO2 slippage-Implementation and Results  
  Amine absorbers in Acid gas Removal units have each 25 valve trays with multiple  liquid feed provisions to Tray No. 2, 4, 6, 8, 10 and 12 and a dry tray at the top. Feed  tray is chosen according to the required selective absorption performance.  
  At the time when SRU Incinerator bellow failure occurred, AGRU Train-1 & 2 were  treating around 10,200 T/D of Sour Raw gas each with about 5,400 T/D of MDEA flow  to Train-1 absorber fed over tray No.4 and 4,700 T/D of MDEA flow to Train-2  absorber fed over tray No.2 to meet the treated gas specification. This has generated an  Acid gas feed flow of approximately 20,500 Sm3/h to SRU.  
  SRU throughput was reduced from 20,500 Sm3/h to 17,000 Sm3/h so as to reduce the  amount of tail gas leaking from the cracked SRU incinerator bellow. This reduction has  created sufficient drop in back pressure in the tail gas section which immediately led to  stoppage of tail gas leak. Due to the above Acid gas feed reduction to SRU, AGRU start  flaring around 3,500 Sm3/h of Acid Gas.  
  To reduce CO2 absorption and to increase CO2 slippage in the treated gas, MDEA feed  nozzle to the absorber column was progressively switched to the adjacent lower ones so  that the number of active trays will be systematically reduced to increase CO2 slippage  in a controlled manner until reaching an optimum beneficial operating point  
  Initially, MDEA feed tray of AGRU Train-1 absorber which operates with  comparatively higher MDEA circulation flow of 5,400 T/D due to pump mechanical  limitation that led to increased CO2 absorption and obviously increased Acid gas flaring  is switched from MDEA feed Tray No. 4 to the next lower MDEA feed Tray No. 6.  Soon after the tray change over, the effect of Acid gas flaring reduction started to appear  positively.  
  MDEA feed Tray of AGRU Train-2 absorber also switched from Tray No.2 to Tray  No.6 and the effect of total 25% drop in flaring became apparent.  
  As the column conditions got stabilized and no further change observed in H2S and CO2  content of treated gas from both AGRUs, it has been decided to proceed further to  switch MDEA feed trays for both the Trains from Tray No. 6 to Tray No.8. This action  increased the CO2 slippage in both MDEA columns considerably and reduced Acid Gas  flaring significantly by more than 80% (see stage 2 in Error! Reference source not  found.).  
  During the mid day period, AGR columns experience significant increase in CO2  absorption due to the increase in MDEA temperature and this led to a marginal increase  in flaring by approximately 3%.  
  After confirming by lab analysis that treated gas composition is well within the accepted  specification limit, AGRU Train-1 feed tray was again changed over from Tray No.8 to  Tray No.10 which almost led to total stoppage of Acid Gas flaring from AGRU.  However, due to the effect of the increased inlet feed gas flow from Al-Shaheen wells  which has a high CO2 content, slippage of CO2 in treated gas has increased together  with marginal flaring due to the excess CO2 absorbed by the amine released in the acid  gas.  
  These conditions were kept under close monitoring for two days and as part of this trial,  periodical Lab analysis carried out for the treated gas and lean gas for H2S and CO2  content, results were found to be positive and product remained on-spec.  
  On the last day of this trial, plant conditions optimized and SRU throughput of Acid  Gas gradually increased from 17,000 Sm3/h to around 18,000 Sm3/h as bellow leak  remained under control and flaring of acid gas completely stopped.  
  
  3. Conclusion  
  Increasing the CO2 slippage in the Amine absorbers has reduced the CO2 content of  Acid Gas considerably and stopped the anti-environmental Acid Gas flaring from  AGRU. This achievement has saved and protected the environment from the impact of  flaring around 300 mmscf of Acid Gas and therefore a loss of around 2610 tons of  liquid sulphur product estimated to be 1.72 MM QR has been avoided.  
  Increasing CO2 slippage in absorber columns has a very minor contribution in change of  lean gas composition, Only the CO2 content has increased from an average of 0.99% to  around 1.4%. H2S content reached a maximum level of 2.0 ppm against 1.0 ppm at  normal condition.  
  
  Flare Reduction Options and Simulation for the  Qatari Oil and Gas Industry  
  Noora AlGhanim, Majeda Khraisheh, Farid Benyahia  
  
  Abstract  
  Flaring and venting are two activities associated with oil and gas production. It is a  combustion process used to dispose gases through vertical stacks or ground flares. Qatar  is a world leader in gas and hydrocarbon processing. It has a world class Ethylene  Cracker, Ras Laffan Olefins Company Limited (RLOC), of 1.3 million mtpa capacity.  RLOC started up in April 15, 2010 and is operated by Qatar Chemical Company  (QChem).  
  Qatar Ministry of Environment (MoE) cap targets flaring rate to less than 1% of inlet  feed gas per year. As part of RLOC compliance with MoE regulations, a study was  conducted, and tested at RLOC. The study is a comparison between the 'Normal'  startup and shutdown procedures with another process called 'Methane Run', which was  followed and suggest by RLOC shareholders from the U.S plants. This paper will  present the tested case study for the purpose of flaring minimization at Ethylene plants  during start up and shutdown and flaring reduction in Qatar and around the world.  This study reveals that 'Methane Run' can significantly reduce flared volumes during  plant startup and shutdown compared to the 'Normal' procedure. Additionally,  'Methane Run' can save two-week of the planned shutdown with a 93% reduction in  cost compared to 'Normal' procedure. Furthermore, 'Methane Run' requires 75% less  costs than the 'Normal' procedure, which makes it preferable by a new operated plant  such as Qchem facility at Messiaed. On the top of its advantages, 'Methane Run' is  environmentally friendly, such that it reduces the CO2 emissions by a minimum of 67%  compared to the 'Normal' procedure.  
  Keywords: Ethylene, flare reduction, startup, shutdown, CO2 emissions.  
  (Continues...)  
     
 
 Excerpted from Proceedings of the 3rd International Gas Processing Symposium   Copyright © 2012   by Elsevier B.V..   Excerpted by permission of Elsevier. All rights reserved. No part of this excerpt may be reproduced or reprinted without permission in writing from the publisher.
Excerpts are provided by Dial-A-Book Inc. solely for the personal use of visitors to this web site.